Maximize jar impact force with additional stretch in the drillstring.
已发表: 06/06/2013
已发表: 06/06/2013
While trying to gain control of a lost circulation zone in the lateral section of a horizontal well in Ward County, Texas, US, the directional BHA became stuck. After 7 hours of working, the 6 1/8-in pipe remained stuck at 12,190 ft, and the operator believed lost circulation material had caused the BHA to stick.
Schlumberger recommended using the Hydra-Jar AP double-acting hydraulic drilling jar in conjunction with the Accelerator AP impact tool for jarring up and down with hydraulic fluid for maximum impact, while protecting the drillstring and surface equipment from damaging shock waves. To ensure optimal placement of the jar and accelerator in the wellbore, an analysis was conducted using the Runner drillstring analysis program.
The drillstring was was backed off at 60° and approximately 11,000 ft. The fish was more than 1,100 ft long. The fishing assembly was tripped in hole to engage the fish, and 25 bbl of PIPE-LAX stuck-pipe additive, from M-I SWACO, a Schlumberger company, was pumped. Then jarring operations commenced.
After only 15 min of down jarring, the stuck BHA was freed and pulled out of the borehole, preventing protracted NPT and allowing the operator to quickly resume normal drilling operations.
Challenge: Recover a 6 1/8-in directional BHA that could not be jarred free at 12,190 ft in a horizontal well section.
Solution: Use a 4.75-in Hydra-Jar AP double-acting hydraulic drilling jar with Accelerator AP impact tool for increased effectiveness, aided by Runner drillstring analysis program.
Results: Freed the stuck BHA after only 15 min of jarring down, significantly minimizing NPT and the associated costs.