Ensure low-rheology drilling fluids without barite sag.
已发表: 12/05/2019
已发表: 12/05/2019
During temporary suspension of a new well, a liner lap started to leak. The well was filled with 1.04-sg [8.66-lbm/galUS] fluid. A 1.74-sg [14.5-lbm/galUS] oil-based drilling fluid failed to kill the well. A pressure buildup test estimated a 2.45-sg [20.4-lbm/galUS] fluid would be required to control the leak.
It was determined that WARP OB CONCENTRATE concentrated colloidal suspension technology could be weighted with MicroBar micronized weighting additive to 2.6-sg [21.66-lbm/galUS] density and remain a workable field-applicable fluid.
The well was displaced with 2.3-sg [19.16-lbm/galUS] WARP OB CONCENTRATE technology. This initial displacement killed the well and was confirmed with a flow check. The well remained stable, and no further density adjustments were needed.